Time to belt up and save energy December 1st 2007 A factory's plan to save energy by upgrading from v-belts to timing belts on air
handling drives has been expanded to include a wide range of automation
equipment.This has cut €140,000 from the annual energy bill, improved the
working environment and suggested further savings
Stryker Orthopaedics
manufacture a range of
orthopaedic implants,bone
cements and bone
substitute materials at it's facility in
Limerick, Ireland. Like many other
companies it has become
increasingly aware of energy cost
increases and has undertaken
several initiatives to reduce energy
usage/costs and to protect the
environment.
Maintenance manager Robert
McKillican calculated that changing
from v-belts to timing belts would
reduce energy consumption by
about 10% and called in Michael
Dineen of Dickson Bearings to
discuss the idea.
It was soon realised that slippage
of the v-belts gave a soft starting
effect,which would be lost with a
toothed belt.The two briefly
considered the use of electronic soft
starts, but soon decided that variable
speed drives would be better because
they could be used to tune the air
handling to exactly match demand.
The plant's eight extraction fans all
worked quite hard to ensure
complete extraction of dust particles.
Initial calculations suggested that
significant energy savings could be
made if each were tuned to exact
local demand, rather than run faster
than necessary.Additionally, staff
numbers and production levels vary
during Stryker's two-shift day so
there was potential to further slow
down the air handling at different
times throughout the shifts.
There were a number of practical
issues to be addressed, not least
which drive to use.Michael
recommended the L300P Series from
Hitachi, three at 55kW and five at
37kW, which are suitable for fan drive
applications.
Meanwhile Robert was
unearthing some practical
considerations.The control panels,
for instance, had to be designed to
fit into a small control room.As they
would be close to some sensitive
equipment, chokes would be
required on every input and output
to minimise noise generation and
harmonics onto the mains.With the
Hitachi drives it was also possible to
set a maximum total output, so that
penalty charges from the electricity
supplier could be avoided. A PLC
would be required to control the
system, and it seemed logical to
stick with Hitachi and use an EH150
series.This communicates with the
plant's existing building
management system to make the
whole installation interactive.
Finally it was realised that security
staff as well as control engineers
would need access to the system.
Therefore it was decided to install
two touch screen HMIs, again
Hitachi, one in the control room the
other in the security office, and to
use clear graphical displays to make
use as intuitive as possible.
Within days of completing the
installation, energy meters
strategically located around the
system were confirming that
considerable savings were being
made.No detrimental effect on
machine performance or other
production compromises were
identified. Initially the drives were
configured to give the fans three set
speeds, but the intention is to
upgrade this with PID pressure
sensor feedback so that load
matching becomes exact.
"For many years we were able to
ignore energy issues, but once we
started monitoring usage our
attitude changed completely," says
Robert McKillican.
"This is now filtering out to the
whole workforce. The lesson is that
monitoring energy consumption
leads to a constant drive for more
savings." |